I need help trouble shooting my 1994 LT1 with EFI connections 24x ignition system. For anyone not familiar, the 24x system converts the LT1 over to the LS1 PCM and ignition system.
Engine details:
355 CID LT1
Compression is 11.3:1
Comp Cams XFI grind 242/248 @ 0.050" lift, 0.584/0.574 lift, 113 LSA, installed at 111 ICL
Stock heads, 3 angle valve job, valve bowls blended and port matched
Ported intake manifold, 58mm throttle body, hooker longtubes, custom y-pipe, and borla cat-back.
This engine has about 2,500 miles on it and ran great before the 24x conversion.
We had this car running great before I installed the 24x system. I installed the 24x components, modified the factory harness for the new components and re-pinned it for the LS1 PCM connectors, and added a set of ford 39 lb/hr injectors all at the same time. Somewhere in that process, something went wrong.
The problem:
Ever since the install we haven't been able to get the LTFTs even close to right. If we have bank 2 LTFT reading at or near 0%, bank 1 LTFT is at +25% and STFT will stay around +15%. If we add more fuel, the left side will go negative as it should, but there difference between the 2 banks stays constant. Bank 2 O2 is staying around 600-700 mv and bank 1 is in the 100-200 range if I remember right.
What I did find last time we added fuel was that after reading the plugs, cylinders 1 and 3 were lean but the rest were all a little rich. I don't know why there is a difference on cylinders 1 and 3. I have no idea what could be causing this issue.
I've talked to Mike at EFI Connections throughout the process. He's been extremely helpful throughout the process. Unfortunately at this point he's as stumped as we are. No one really has any explanation for what this car is doing.
So far, we've been through the following multiple times and have seen no change:
-All of the sensors and connectors have been checked to go to the right PCM pin
-Every wire that should have voltage has the proper voltage
-Every ground has been checked
-Every wire has been checked for continuity
-Plugs changed
-Plug wires checked with no issues
-Checked for exhaust leaks everywhere
-O2 sensors replaced
-Intake gaskets replaced
-Adjusted the rockers
-Swapped coils
-New injectors
-Leak down test and it was perfect
-Compression tested and all cylinders checked fine
At this point I can only come up with 2 possible causes that I haven't verified yet:
1)The injector wiring, being 17 years old, may have some internal breaks from being manipulated when I re-worked the harness and may not be firing the injectors properly every time.
2)The crank reluctor could have been machined wrong somehow. I'm going to check crank signal with an oscilloscope at work to verify that it is getting the proper signal. I hope this isn't the issue because EFI connections has basically told me if the reluctor is the problem, I'm basically shit out of luck and have to buy a new one (for $250).
Has anyone ever seen any issues like this with fuel trims? Does anyone have any suggestions where I can go from here?