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Thread: Help Still no boost

  1. #1
    Tuner copley87blazer's Avatar
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    Help Still no boost

    Ok here it is. Work on Ve as others have said, runs a ton better but still cant build more than 1 psi of boost.

    5.3 stock
    home built hot side, pressure tested
    jgs 50mm wastegate 7psi spring
    pt74gts 81 ar exh 3'' Dp 2 1/2 crossover
    60lb dekas
    2bar sd
    frt mnt intercooler 3'' cold pipe with t bolts
    Th350 with nitrouse converter built 2600 and 3200 in juice

    I have tried everything iam running 93 with 110 mix 50/50 should be around 101 oct No cats. Pulls hard like a 12 sec car but should be closer to a low 11. Its a 2wd blazer 87 around 3000 me in it ford 8.8 and 355 gear. Im lost I will post log tune and config thanks.

  2. #2
    Tuner copley87blazer's Avatar
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    Do I not have enogh timing should be ok and build boost it hits 1psi then stops wtf

  3. #3
    Senior Tuner Google's Avatar
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    From 105 kpa to 110kpa you drop the amount of fuel your adding.. Over 100kpa is boost.. You have no wideband in the log. I would guess your leaning it out to much.. Take your vacuum line off the waste gate and run spring pressure and you should be able to run 7psi.. Now this is to help figure out a few things... 1. If it is a wastegate control issue or a fuel issue. 2. You also need to correct your P121 & P106 errors to keep out of reduced power mode.. 3. Your trying to use boost enrichment and should just stick with pe enrichment as B.E. is for fail safe as well as the switch causes a lean spike. What BOV setup are you running? What plugs are you using and the gap?

    Let us know if any of this helps..


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  4. #4
    Tuner copley87blazer's Avatar
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    Thanks google My wb reads 11.3 at wot hmm I will try these things you listed thanks

  5. #5
    Tuner copley87blazer's Avatar
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    Ok google had my wg and bov refranced off of infake, well dissconected wg and well went to 7 psi Should I come sraight from compressor housing. I guess wg is too big wtf had too small of one before now have too big. I guess I can change spring to heavy one but then im worried about spike.

  6. #6
    Senior Tuner Google's Avatar
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    What boost controller are you using? Electric or manual boost controller? or just plugged into the intake?


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  7. #7
    Tuner copley87blazer's Avatar
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    Just have it pluged into intake no boost controller

  8. #8
    Senior Tuner Google's Avatar
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    Quote Originally Posted by copley87blazer View Post
    Just have it pluged into intake no boost controller

    Thats your problem.. Get One and then you will be fine! In the meen time just run off spring pressure..





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  9. #9
    Tuner copley87blazer's Avatar
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    Thanks google